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In a recent HAZOP study for an agrochemical plant, our team at HSE Risk Management Services Pvt. Ltd. identified a critical hidden risk in the distillation & solvent recovery system.

At first glance, the process appeared routine.However, during detailed HAZOP discussions with the plant team, key concerns emerged:<br>

⚠️ Increasing concentration of residue during solvent recovery<br>⚠️ Elevated temperature and pressure conditions<br>⚠️ Potential thermal instability under abnormal scenarios

🔍 What changed the game?

We went beyond conventional HAZOP by integrating ARC & DSC thermal study data.

The findings were significant:

  • Exothermic decomposition starts at ~140 °C
  • Severe secondary decomposition near ~240 °C
  • Potential for runaway reaction and high pressure rise (~140 bar)

💡 Critical Insight

A proposed shift to a higher temperature utility (180–190 °C) could push the system dangerously close to decomposition conditions.

👉 This would have reduced the safety margin to near zero.

Final Outcome

Based on our integrated analysis, we recommended:

✔ Use of Low Pressure Steam (LPS) only<br>✔ Limiting reactor temperature to ≤ 130 °C<br>✔ Avoiding high-temperature utilities for this system

🎯 Why this matters

This study reinforced a key process safety lesson:

Distillation is not always just separation—residue behavior can introduce serious thermal risks.

And more importantly:

Heating medium selection is a safety decision, not just an operational choice.

🔗 If you're working with distillation, solvent recovery, or reactive systems, this is a reminder to always combine:<br>✔ Process understanding<br>✔ HAZOP analysis<br>✔ Thermal stability data

About Yashpal singh

Mr. Yashpal Singh is the Managing Director and Process Safety Expert at HSE RMSPL. With 19 years of experience, he specializes in HAZOP, QRA, and functional safety engineering. He helps clients achieve safe, compliant operations while minimizing industrial risks and incidents.

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